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Problem
solved
Compressed
air optimization saves energy, improves production at forging plant
The
Interstate Forging unit of Citation Corporation implemented a
compressed air system improvement project at its Milwaukee forging
plant.
The
project enabled the plant to maintain an adequate and stable pressure
level using fewer compressors, which led to improved product quality
and reduced
production downtime. The project also yielded annual compressed air
energy savings of 820,000 kilowatt-hours (kWh) and $45,000, plus
better maintenance scheduling.
With
a total project cost of $67,000, the plant achieved a simple payback
of 1.5 years. In addition, the project’s success established that no
need existed to buy a new compressor. This resulted in avoided capital
costs of roughly $60,000 for a new 200-horsepower (hp) unit.
Why
did they do it?
Compressed
air is vital to Interstate Forging’s production process because it
supports grinding and pressing applications as well as the drop-forge
hammers necessary
to manufacture various parts. The forging hammers are the most
important compressed air application, and require a consistent
pressure level of 95 pounds per square inch gauge (psig) to achieve
reliable production. Prior to the project, plant operators tried to
maintain a system pressure of 100 psig by running five compressors
totaling 900 hp that generated up to 3,500 standard cubic feet per
minute (scfm) at a discharge pressure of 105 psig.
Despite
operating all five compressors and using a 2,500-gallon storage
receiver, the system pressure fluctuated between 85 and 100 psig. The
pressure fluctuations caused the drop-forge hammers to operate
erratically, reducing product quality and increasing cycle time.
Convinced that additional compressors were necessary, plant management
brought in a U.S. Department of Energy resource partner to review the
compressed air system. This resource’s role was to determine how
much additional capacity was needed to eliminate the pressure
fluctuations and to improve the system’s performance.
However,
the resource found that the plant could establish and maintain the
required system pressure by operating fewer compressors. The
hammers’ intermittent air demand and insufficient compressed air
storage were the main causes of the pressure fluctuations at points of
use.
Another
problem was an air leakage rate of about 20 percent of system output.
Most of the air leaked from counterbalance cylinders in the hammers,
from point-of-use applications and from some of the system’s
distribution piping. The air leakage created artificial air demand,
which made the compressors work harder to generate the needed air
volume.
How
did they do it?
Following
the system review, plant personnel implemented a system-level project
designed to allow the compressed air system to function effectively
without the need to buy additional compressors. The first measure was
to stabilize system pressure at the lowest level that met production
requirements. To do this, plant personnel installed
a pressure/flow controller (P/FL) to separate the demand side of the
system from the supply side. In addition, they installed 5,000 gallons
of compressed air storage capacity just upstream of the P/FL.
Compressed air was set to flow into the storage receivers at 100 psig
and to be released into the main header at 95 psig, plus or minus 1
psig.
Next,
plant personnel initiated an innovative leak detection and repair
campaign. In addition to finding and repairing the largest leaks in
the distribution piping, plant personnel redesigned the shaft seals on
the counterbalance cylinders so that repairing leaks on those
cylinders could be accomplished without having to disassemble the
cylinders. This redesign greatly simplified the task of repairing
leaks on those pieces of equipment. They also decided to repair leaks
on a daily basis instead of waiting until semi-annual maintenance
shutdowns.
Conclusion
This
compressed air system project yielded important energy savings,
improved system performance and enhanced productivity. Currently, the
plant operates effectively with three 200-hp compressors, whereas
before the project it was unable to meet its air demand while
operating five compressors totaling 900 hp at full capacity. The
system pressure has been stabilized and lowered to 95 psig, and the
remaining compressors (one 200-hp and one 100-hp unit) now serve as
backup compressors. The stable air supply has reduced production
downtime and improved product quality.
The
leak repair effort has reduced artificial demand by almost 600 scfm,
lowering the average system flow rate. The system’s average air
demand has declined from between 3,000 and 3,500 scfm to between 2,400
and 2,600 scfm.
That’s
a significant compressed air improvement!
This
article was reprinted with permission from Energy Matters, a quarterly
newsletter published by the United States Department of Energy’s
Industrial Technologies Program.
This article appeared in
the April/May 2004 issue of MRO Today magazine. Copyright 2004.
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